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Old Nov 15, 2012 | 04:37 PM
  #16  
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Ya I meant stripping the splines haha I already started pulling it again just really hoping in didn't mess up the pump and tq converter I checked it with a strait edge to make sure it was seated but who knows thanks for the response I knew it had to come out I just didn't want to admit it to myself yet
 
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Old Nov 15, 2012 | 05:04 PM
  #17  
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Haha ya i meant strip the pump splines Thanks for your response I already started pulling it again I pretty much knew I messed something serious up I just didn't want to admit it I kinda doubt that's what happened cause I checked that it was seated with a strait edge
 
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Old Nov 15, 2012 | 07:06 PM
  #18  
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From: Semper Fi tell I die!
i like strippers.
 
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Old Dec 2, 2012 | 04:32 AM
  #19  
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I finally got around to pulling it out again and I didn't damage the pump I'm gonna tear into it tonight
 
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Old Dec 5, 2012 | 12:00 AM
  #20  
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I got it pulled and broken down no obvious damage the only thing I saw was there is a small scratch on th overdrive piston not sure if that could be causing my line pressure issue
 
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Old Jan 12, 2013 | 12:58 AM
  #21  
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I finally got it running and figured out what I did wrong I put the little mesh filter into the valve body spacer plate before I put the gasket on which caused a cross leak in the valve body which I think is what caused my pressure issues
 
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Old Jun 28, 2013 | 08:02 PM
  #22  
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Well I let the truck sit for three months and now it won't move try's to shift into gear I thought it was just the brakes locking up so I jacked it up and they are free checked fluid level looks good I haven't dropped the pan or anything to see what's up yet
 
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Old Jul 13, 2013 | 02:41 PM
  #23  
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I hooked up a pressure gauge and have 60 psi in park so I'm guessing something mechanical must be broken just looking for another opinion before I rip it apart again
 
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